Nov 02 2012

An emergency landing at Charleston

Day was an interesting day for in my fruitless search for the engine problem.

I had completed four flights today. What I discovered was I could not get any power above 2480 RPM. When I went full throttle engine actually started running rough and backfiring. I called Klaus at Lightspeed to discuss the problem and he stated focusing me and on the fuel flow. It is too low. I am only seeing about 9 gph and at full throttle and it should be up to 12 gph. Humm, maybe that is one of the problems.

After talking to Klaus, I decided to take it up for another test flight. As I was climbing out the fuel flow initially I went up to 11.8 gallons per hour, then the fuel flow dropped to 7 gallons per hour and I started losing power. I declared an emergency and they had to divert a airliner landing to get me on the ground in a hurry. What fun! NOT!

I called Airflow Performance back (which built my fuel injection system,) talk to the owner Don, and we decided I could bring the system to Greenville testing on Tuesday. I had already cleaned two filters, but was unaware that there is a third filter in the system.

This is the fuel servo (1 filter in it)

wpid-CIMG1590-2012-11-2-15-48.jpg

This is the flow spider (it also has a filter).

wpid-CIMG1589-2012-11-2-15-48.jpg

Cant wait to see what the initial test results show up.

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